General information

IMO:
9610092
MMSI:
241166000
Callsign:
SVBM6
Width:
32.0 m
Length:
190.0 m
Deadweight:
Gross tonnage:
TEU:
Liquid Capacity:
Year of build:
Class:
AIS type:
Cargo Ship
Ship type:
Flag:
Greece
Builder:
Owner:
Operator:
Insurer:

Course/Position

Position:
Navigational status:
Moving
Course:
148.0° / 0.0
Heading:
150.0° / 0.0
Speed:
Max speed:
Status:
moving
Area:
Gulf of Thailand
Last seen:
2025-09-05
14 hours ago
Source:
T-AIS
Destination:
ETA:
Summer draft:
Current draft:
Last update:
16 hours ago
Source:
T-AIS

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Latest ports

Port
Arrival
Departure
Duration
2025-09-02
2025-09-05
2d 12h 3m
2025-06-12
2025-06-13
1d 6h 41m
2025-05-05
2025-05-07
2d 13h 58m
2025-04-16
2025-04-27
10d 20h 14m
2025-04-10
2025-04-12
1d 16h 4m
2025-04-05
2025-04-10
4d 10h 13m
2025-03-20
2025-04-05
16d 13h 46m
2025-03-10
2025-03-16
5d 14h 12m
2025-02-17
2025-02-21
3d 11h 44m
2025-02-14
2025-02-15
1d 4h 36m
Note: All times are in UTC

Latest Waypoints

Waypoints
Time
Direction
Cape Town
2025-07-17
Enter
Canary Islands
2025-06-26
Enter
Dover
2025-06-20
Enter
Calais
2025-06-20
Enter
Skagen
2025-06-17
Leave
Läsö DK
2025-06-17
Leave
Anholt
2025-06-17
Leave
Note: All times are in UTC

Latest news

NTSB report into allision published

Fri Aug 29 13:35:18 CEST 2025 Timsen

The National Transportation Safety Board concluded in an investigation into an allision in the Houston Ship Channel on Aug 25, 2023. The cargo m/v 'BBC Africa' (IMO: 9362621) was departing Houston, Texas, on that day, when the vessel suddenly lost steering control and veered off course, striking the docked 'Common Faith', which was berthed at the Anderson Grain Terminal in Houston. The post ballast tank of the vessel was punctured, along with damage to the shell plating, which cost a total of $467,000 to repair. The 'BBC Africa' suffered damage to its bulbous bow, hull, and shell plating and forward bulwarks, costing $700,000 to repair. There were no injuries or pollution reported from the incident. The NTSB reconstructed the events using AIS data and crew interviews. The 'BBC Africa'’s VDR was not functioning, but the vessel had permission to sail while repairs were being arranged. On the morning of Aug 25, pre-departure testing of the system on the 'BBC Africa' showed no problems. The 2nd officer tested the steering gear, checked rudder movements, and ran the steering gear pumps, while engineers also completed a pre-departure checklist. The master also tested steering from the port bridge wing and told the pilot aboard that everything was “in good working order.” About 10 minutes after having gotten underway, the ship was making speeds up to 6.8 knots, and everything was going smoothly. The pilot released the escort tug, and the pilot and master ordered that maneuvering control (bow thruster, main propulsion engine control, and steering) be transferred from the port bridge wing to the main control station on the bridge. The chief officer pressed the button to activate the controls on the bridge. The pilot then gave a command for starboard 10, and the helmsman confirmed adjusting the rudder. Sensing the vessel was not turning at the expected rate, the pilot ordered starboard 20 and then hard to starboard. It was then that the chief officer realized the indicator light on the main control station had gone off and tried pressing it several times to reengage the controls. The rudder indicator was showing a hard port position of 30 degrees. The master then switched the vessel’s steering to emergency override mode and got the rudder back to 30 degrees starboard. The pilot also ordered full astern, and the master then put the bow thruster to 100 percent starboard thrust. However, it was too late, and they hit the docked bulker. The investigators were unable to replicate the failure, but working with the system manufacturer determined that a component failure had caused the system to fail. The company’s investigation found the rubber on the joystick (tiller) had invisible cracks that let moisture into the control unit, which contributed to the loss of the electrical signal. The shipping company, on advice from the manufacturer, changed the bridge wing steering control tillers, the “in command” push buttons, and the main power supply transformer. They made the same changes on two other vessels with similar control systems. According to the report the primary cause was the equipment failure. However, they also noted a stressful situation with short reaction time due to the vessel being in the confines of the port. The NTSB noted that the crew had gone through training and regular drills, but recommended further training, saying that the delayed response from the ship’s crew to implement the emergency steering procedure from the bridge contributed to the vessel striking the docked bulker. The steering gear manufacturer also issued a safety bulletin. It highlighted incidents with systems manufactured between 2002 and 2009, noting that they had malfunctioned due to a weakness with the protective rubber and the micro switches. The bulletin said the consequence of the failing micro switches could lead to unintended rudder movement.

New Charter fixed

Mon Feb 13 21:49:45 CET 2017 arnekiel

delivery U.S. Gulf spot, redelivery Northern Spain, intention petcoke, 15.000 $ daily, XO Shipping

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Daily average speed

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Distance travelled

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Ship master data